AIDA GELINA BRIKEN nToF CRIB ISOLDE CIRCE nTOFCapture DESPEC DTAS EDI_PSA 179Ta CARME StellarModelling DCF K40
  CARME, Page 27 of 33  ELOG logo
  ID Date Author Subject
  135   Sun Oct 31 07:41:20 2021 CB JM + RSSWires plugged in DSSDs

(Wed 27 October)

Started with top-most flange. Attemptedto plug in MACOR lead in DSSD plug in preparation for jacking in. Realised that extender plate thickness causes plug to be rasied with respect to nominal position, which results in plug non entering straight. Removed extension plate.

Plugged MACOR lead in. OK. Inserted M6 jacking bolts and gently turned by hand. No resistance until jacking action starts. Jacked plug in with spanner and even 1/4 turns. Removed bolts. All OK.

Attempted same with bottom-most cable harness. Due to strain from top-most wire harness the plate is now rotated on the rod. Rotated back. Jacked in. Removed bolts. No issues.

MACOR plugs show small gap in rear part. Gap seems due to harness strain and disappears depending on plate orientation. Will check but pins are obviously connected.

 

(Thu 28 October)

Attempted to plug in top-left MACOR lead. Dog leg conflicts with jacking screw! Only solution is to slacken bolt, rotate strut, fasten again with detectors still on plate. Result attached. No clear if design, manufacturing or mounting oversight.

Had to attemping plugging in a few times before jacking bolts went in straight (i.e. no resistance felt). Jacked in both leads. No further issues.

Gap appears less significant in newly plugged leads. probably as a result of lack of rotational freedom.

 

Attachment 1: 20211027_184502.jpg
20211027_184502.jpg
Attachment 2: 20211027_184527.jpg
20211027_184527.jpg
Attachment 3: 20211027_184535.jpg
20211027_184535.jpg
Attachment 4: 20211028_105802.jpg
20211028_105802.jpg
Attachment 5: 20211028_105919.jpg
20211028_105919.jpg
Attachment 6: 20211028_105711.jpg
20211028_105711.jpg
Attachment 7: 20211028_105728.jpg
20211028_105728.jpg
Attachment 8: 20211028_105734.jpg
20211028_105734.jpg
  134   Sun Oct 31 07:29:17 2021 CB JM + RSS OGDetectors mounted on plate in CARME

(Wed 27 October)

Dismounted plate from rod. Dismounted broken detectors from plate and placed back in box. Dismounted "dog leg" struts and replaced with fully un-threaded struts.

Mounted 3335-13 in bottom position.

Attempted to mount 3335-2 in top position: dog leg strut conflicts with jacking plate. Attempted to remove - bolt stuck in thread. Removed bolt with great difficulty after dousing the bolt and hole in ethanol. M3 vented bolt is completely bent. Thread in hole appears still good. Bad bolt? Mounted strut upside-down with new M3 vented bolt. No issues. Mounted 3335-2 on plate.

Mounted extension plates for strain relief. Note countersunk bolts.

Removed all flanges with wires from CARME. Lubricated rod with ethanol. Slid rod with 2x detectors on. FIxed with bolt in front and back. Plate securely mounted in CARME, but some degree on rotational freedom is left.

Attachment 1: 20211027_172114.jpg
20211027_172114.jpg
Attachment 2: 20211027_172114.jpg
20211027_172114.jpg
Attachment 3: 20211027_172124.jpg
20211027_172124.jpg
Attachment 4: 20211027_172132.jpg
20211027_172132.jpg
Attachment 5: 20211027_172138.jpg
20211027_172138.jpg
Attachment 6: 20211027_175255.jpg
20211027_175255.jpg
Attachment 7: 20211027_175308.jpg
20211027_175308.jpg
Attachment 8: 20211027_174610.jpg
20211027_174610.jpg
  133   Sun Oct 31 07:21:09 2021 CB JM RSSDetectors arrived in GSI

(Tue 26 October)

Two new CARME DSSD arrived in GSI and collected. Visually inspected both sides. No obvious damage. Photos attached. Second detector (3335-2) was shipped in upside-down box. Does not seem to have made any difference.

3335-13 will be mounted on bottom of plate. 3335-2 will be mounted on top of plate.

 

Attachment 1: 20211026_144342.jpg
20211026_144342.jpg
Attachment 2: 20211026_144656.jpg
20211026_144656.jpg
Attachment 3: 20211026_145204.jpg
20211026_145204.jpg
Attachment 4: 20211026_145206.jpg
20211026_145206.jpg
Attachment 5: 20211026_150432.jpg
20211026_150432.jpg
Attachment 6: 20211026_150727.jpg
20211026_150727.jpg
  132   Fri Oct 29 15:09:27 2021 CB JM + RSS OG DRPreparation to mount new DSSDs

(Mon 25 October - Tue 26 October)

Considered different strategies to mount DSSDs inside CARME, while waiting for 2x new DSSD to arrive.

Plan A: Mount DSSDs on plate on the bench, slide plate on rod, then attach cables, then attach strain relief

Plan B: Mount DSSDs on plate, attach cables, attach strain relief, slide plate on rod, connect cables to feedthroughs

 

Mounted detectors on plate using new "dog leg" connectors. Threaded and unthreaded holes are flipped! Asked DR to unthread hole in two out of four, and clean.

 

Attempted to proceed with Plan B with stand-in broken detector. Found even a single wire harness attached to the detector was quite hard to insert in the chamber. Temporarily dismounted left-hand 2x UHV1400 to give more space.

Slid plate on rod. New position of rod block makes it easier to mount. Spraying ethanol on the rod to lubricate also helps greatly. Secured plate to rod. Holding flange with cables in left hand, attempted to mount macor plug in feedthrough with right hand. Unable to exert sufficient strength (CB, JM, OG). Pulling on the cable puts strain on the DSSD. Decided to avoid.

 

Attempted Plan A. Jacked connector in with no issues using M6x40 partly threaded bolts. Unable to unjack due to part threads! Obtained fully threaded rods. Unjacked using washer + two nuts tightened on each other. Jacked and unjacked another connector.

Decided to proceed with A. Having any cable pre-mounted in the chamber is a potential hazard to the detectors while mounting plate. Decided to dismount all flanges, re-organise harnesses and mount one flange+harness at a time after mounting detector on rod.

 

Used thick Kapton coated Cu from NEG pumps to organise the cables and improve strain relief.

Due to width of MACOR strain relief and nuts on the back of the MACOR plugs, realised strain relief cannot be mounted as intended. Asked DR to produce 90 x 30 x 3 mm extender plates instead. MACOR strain relief are 15 mm wide. Extender plate have 3x M4 unthreaded countersunk to fix to detector plate, 3x M4 threaded holes to hold MACOR strain relief.

 

Organised cable harnesses.

4 short: all good -> two to be mounted

2 long: all good -> to be mounted

1 long: Broken MACOR backplate and lead. Lead removed. Attempted to mount with backplate in new lead - unable to do so. Removing backplate requires re-crimping. Will have to send back to Edinburgh

1 long: Wires cross in odd way. Will have to re-organise. Probably requires re-crimping. One pin smashed during jacking. Not sure if rescuable. See attached.

 

Attachment 1: 20211025_104612.jpg
20211025_104612.jpg
Attachment 2: 20211025_161821.jpg
20211025_161821.jpg
Attachment 3: 20211025_161804.jpg
20211025_161804.jpg
Attachment 4: 20211026_161756.jpg
20211026_161756.jpg
Attachment 5: 20211026_163113.jpg
20211026_163113.jpg
Attachment 6: 20211026_163202.jpg
20211026_163202.jpg
  131   Sat Oct 23 12:58:11 2021 JMGSI vacuum and bakeout testing summary

Attachment 1 shows the pump-down of the CARME chamber at GSI before installation of kapton cabling inside the chamber and mounting of the chamber on the ring. Discontinuity in the plot is from switching between the pirani gauge and IE514 gauge. The pumping of the chamber in the turbo regime follows the power law where P ~ 1/(nt) due to outgassing from the chamber being dominated by water outgassing which has an n ~1 dependence (for first order desorption). This is seen in the pumping of the chamber in the turbo regime (Attachment 2) where pressure falls with an n of 1.03. In red the power law is extended to 10^5 minutes, demonstrating the limitations of pumping the chamber without baking. 

Attachment 3 shows the pumpdown pressure and baking temperature (chamber average) of the chamber once mounted on the ring, with all kapton installed in the chamber. Temperature data was lost in the middle of the plot due to the power cut to CRYRING causing temperature data to not be saved to the pi. Some of this data was plotted in elog 87 before beong lost from the pi. Points on the graph correspond to:

Point 1 - Baking started 2pm 23/9/21

Point 2 - Temperature limited to 40C due to high thermal gradients from uneven baking of the volume. Baking stopped 7am 24/9/21 so that heating elements could be repositioned. Baking restarted 10am.

Point 3 - Baking limited to 90C due to tent construction. Negative gradient detected due limitation causing baking to stop around 5pm 25/9/21. Manual mode to 60C. Full power mode restarted 10pm

Point 4 - Temperature of the volume reached 100C. 11am 27/9/21 baking stopped to install new turbo sections. Baking restarted at 3:25 pm Temperature peaks at 130C next morning.

Point 5 - 29/9/21 10am Unexpected power cut at CRYRING, temperature fell to 120C power restored shortly after.

Point 6 - 4/10/21 9am Temperature reduced to 100C and ion pumps outgassed. Activation of NEG pumps

Point 7/8 - Subsequent activation of other NEG pumps.

Point 9 - 7/10/21 CARME reached 9E-12 mbar. Gate valve closed, pressure rises with apparent floor at 1.5E-11 mbar

Some variations in the pressure are seen after reaching the floor, most likely due to sputtering of ion pumps. 

Teething problems with the bakeout such as heater placement and new jacket sections in addition to the power cut prevented continous bakeout for entire period, these issues should not affect the next baking run. As a result of the slightly fractured bakeout the pumpdown power laws have been plotted (logP) against log(T) in sections where temperature was roughly constant with the associated timestamps to gauge the decrease in pressure over time using this power law (Attachment 4). 

Room temp  n ~ 0.75

90C n ~ 9.15

130C (1) n ~ 8.05

130C (2) n ~ 7.37

130C (3) n ~ 4.89

130C (4) n ~ 2.65

Introduction of kapton cabling likely causes change to scaling as the diffusion of gas from kapton not the desorption from the surface dominates the outgassing rate. Diffusion has an n ~ 0.5, likely contributing to the change between the blank chamber and mounted chamber. As the temperature is increased the outgassing is significantly increased causing an initial increase in the temperature followed by a more rapid decrease in the gradient of the pressure decrease over time than at lower temperatures. As time increases, outgassing from water in the chamber dominates less and less with the kapton cabling representing a more significant portion of the total outgassing load likely causing the decrease in n as time increases despite baking at 130C. After ~12000 minutes n decreases significantly and more variations from the linear decrease in pressure are observed. After 17000 seconds the pressure begins to plateu and reached a floor of ~1E-7 mbar over the weekend at which it was assumed outgassing from water in the chamber was no longer significant. Variations could be due to temperature fluctuations which had a greater impact on the pressure as the pressure began to reach the floor.

Activation of NEG pumps was conducted after reaching the floor. The average chamber temperature and air temperature inside the tent was unaffected by the activation of NEG pumps, however the internal thermocouples significantly increased during activation (attachment 5). The internal thermocuples were largely unaffected by the NEG activation until the NEG temperatures were themselves above ~300C after the internal temperatures rose rapidly (more detail in elog 105,108,109,110) . Activating so many NEG elements at once is thus not feasible as temperatures would damage the detectors once mounted. Activating one group at a time (typically 2 NEGs) and D2000's which are away from the detectors to start with and then maintaining at low power before slowly activating NEG's close to the detectors perhaps at a lower temperature will be done to keep temperatures below 130C. A full activation procedure will be posted to the elog before activating again.  

Attachment 1: GSI_fullpumpdown.png
GSI_fullpumpdown.png
Attachment 2: GSI_pumping.png
GSI_pumping.png
Attachment 3: Bakeout-elog.png
Bakeout-elog.png
Attachment 4: fit-elog.png
fit-elog.png
Attachment 5: Activation-elog.png
Activation-elog.png
  130   Fri Oct 22 13:22:48 2021 TDCARME FEE64 adaptor PCB
Attachment 1: 3D.pdf
3D.pdf
Attachment 2: Bottom_Ground_Pad.pdf
Bottom_Ground_Pad.pdf
Attachment 3: Flex_Layer_1.pdf
Flex_Layer_1.pdf
Attachment 4: Flex_Layer_2.pdf
Flex_Layer_2.pdf
Attachment 5: Flex_Layer_3.pdf
Flex_Layer_3.pdf
Attachment 6: Flex_Layer_4_(1).pdf
Flex_Layer_4_(1).pdf
Attachment 7: PCB_Bottom.pdf
PCB_Bottom.pdf
Attachment 8: PCB_Top.pdf
PCB_Top.pdf
Attachment 9: Silkscreen_Top.pdf
Silkscreen_Top.pdf
Attachment 10: Top_Ground_Pad.pdf
Top_Ground_Pad.pdf
  129   Fri Oct 22 13:11:26 2021 TDMSL type TTT14 assembly drawings & pin assignments
Attachment 1: C-3434.pdf
C-3434.pdf C-3434.pdf C-3434.pdf C-3434.pdf
Attachment 2: C-3517.pdf
C-3517.pdf C-3517.pdf C-3517.pdf C-3517.pdf C-3517.pdf
  128   Thu Oct 21 20:26:44 2021 JM TDThermocouple and Connector cables

NEG pump electrical connections tested - all connections sound. 

Detector carriers have been redrilled and are currently being cleaned. Carriers were checked within the chamber, mounting much easier with new hole. Distances to NEG feedthroughs and thermocouple feedthrough from the carrier also checked. NEG feedthroughs have sufficient separation now moved, thermocouple required moving to top flange position to avoid collision with carrier. 

Longer external thermocouples required for top position to reach TC08's. 3 Longer thermocouples made up using spare wire and connected to feedthrough. All thermocouples checked using baking code - all appear fine. We have 2 long thermocouples for the interaction chamber, 2 for the RE-72's and one for the top of the chamber left. Bellows can be reached by shorter thermocouple. This should be sufficient for baking. 

Standoffs job submitted to workshop for production, may be available end of the week depending on schedules of workshop. Clamp guide and hook tools produced.

Cable connectors have started to be seperated and bound into 16 and 17 cable bunches to enable a good fit in strain reliefs. Upon inspection D-connectors were attached upside down and required flipping to correct position (see image - thumbs up indicates correct position). Cables fit through funnel strain reliefs well, other strain reliefs look more difficult - may require more hands to complete. One long connector has criss crossed wires which may not fit in strain reliefs and may require re-wiring a few cables and one long has broken D-connector. Broken ceramic can be replaced with new D-connector and other long connectors are available

Damaged detector removed from carrier and is in its box - awaiting delivery of other detectors. 

Interaction chamber mounted on its frame in CRYRING as well

 

Attachment 1: 20211021_111319.jpg
20211021_111319.jpg
Attachment 2: 20211021_173047.jpg
20211021_173047.jpg
Attachment 3: 20211021_142901.jpg
20211021_142901.jpg
Attachment 4: 20211021_173102.jpg
20211021_173102.jpg
Attachment 5: 20211021_173107.jpg
20211021_173107.jpg
Attachment 6: 20211021_173054.jpg
20211021_173054.jpg
Attachment 7: 20211021_173047.jpg
20211021_173047.jpg
Attachment 8: 20211019_114556.jpg
20211019_114556.jpg
Attachment 9: 20211021_100650.jpg
20211021_100650.jpg
Attachment 10: 20211021_111516.jpg
20211021_111516.jpg
  127   Mon Oct 18 16:25:11 2021 JM RSS TDNEG rotation + cable removals

Kapton cabling and the broken ceramic detector holder have been separated. Required holding jacking plate in a vice and using lots of propanol to wet the jacking screw. A long set of kapton cabling has been removed from the other side of the chamber which can be used when mounting the detectors. The feedthrough flange was re-mounted on that side with no kapton cabling. 

The wiring for the NEG feedthroughs was in confilct with detectors in previous position. Feedthroughs have been moved to the DN40 flanges at the top and bottom of the chamber section. In order to wire the NEGs to the feedthroughs required rotating the NEGs one position anti-clockwise and re-wiring some of the connections. 

Left two Getters are connected in series and are connected to the top feedthrough. The two right and the bottom getter are connected in series and are connected to the bottom feedthrough

Attachment 1: Screenshot_20211018-174141_Signal.jpg
Screenshot_20211018-174141_Signal.jpg
Attachment 2: 20211018_111130.jpg
20211018_111130.jpg
Attachment 3: 20211018_100015.jpg
20211018_100015.jpg
  126   Sun Oct 17 11:48:48 2021 TD RSSSunday 17 October
Looking downstream the RHS motor assembly has  loose green/yellow (gnd?) see attachment 1

Install blank base plate to trial install in downstream CARME chamber. The rod is just through all of the mounting holes - see attachments 2 & 3

The rod, plate and block are close fitting.

The current position of the TC feedthrough is incompatible wit detector movement- the TC feedthrough should be moved.

Detector baseplate with 1x DSSSD installed - attachments 4 - 6, Cabling length looks OK. 

Should move NEG power and TCs to top & bottom DN40 flanges to avoid conflicts with DSSSDs and cabling.
Attachment 1: 20211017_124717.jpg
20211017_124717.jpg
Attachment 2: 20211017_130436.jpg
20211017_130436.jpg
Attachment 3: 20211017_130447.jpg
20211017_130447.jpg
Attachment 4: 20211017_133051.jpg
20211017_133051.jpg
Attachment 5: 20211017_133105.jpg
20211017_133105.jpg
Attachment 6: 20211017_133229.jpg
20211017_133229.jpg
Attachment 7: IMG_5146.JPG
IMG_5146.JPG
Attachment 8: IMG_5145.JPG
IMG_5145.JPG
Attachment 9: IMG_5144.JPG
IMG_5144.JPG
Attachment 10: IMG_5143.JPG
IMG_5143.JPG
Attachment 11: IMG_5142.JPG
IMG_5142.JPG
Attachment 12: IMG_5141.JPG
IMG_5141.JPG
Attachment 13: IMG_5139.JPG
IMG_5139.JPG
Attachment 14: IMG_5140.JPG
IMG_5140.JPG
  125   Sat Oct 16 17:25:47 2021 RSS TDBroken detectors

One of the detectors was damaged while mounting (see pictures 1-3).

Second detector was found already damaged when opened (see pictures 4-5).

Attachment 1: IMG_5098.JPG
IMG_5098.JPG
Attachment 2: IMG_5097.JPG
IMG_5097.JPG
Attachment 3: IMG_5096.JPG
IMG_5096.JPG
Attachment 4: IMG_5106.JPG
IMG_5106.JPG
Attachment 5: IMG_5105.JPG
IMG_5105.JPG
  124   Fri Oct 15 19:37:12 2021 RSS TD + DRFriday 15 October

Ring seal is out. See picture 1.

Bellow (towards CARME) was installed in the gas jet chamber. Attached are some pictures.

Attachment 1: IMG_5059.JPG
IMG_5059.JPG
Attachment 2: IMG_5060.JPG
IMG_5060.JPG
Attachment 3: IMG_5061.JPG
IMG_5061.JPG
Attachment 4: IMG_5062.JPG
IMG_5062.JPG
Attachment 5: IMG_5064.JPG
IMG_5064.JPG
Attachment 6: IMG_5068.JPG
IMG_5068.JPG
Attachment 7: IMG_5071.JPG
IMG_5071.JPG
Attachment 8: IMG_5073.JPG
IMG_5073.JPG
  123   Thu Oct 14 15:54:47 2021 TD RSSThursday 14 October
Attachment 1 - what is function of the 4x c/s holes indicated?


DSSSD install sequence

1 add 136 - 2x78 way cable harnesses to DSSSD mount via strain relief

2 add DSSSD to mount

3 connect 136 D connector

4 install in CARME chamber 

5 connect 2x78 D connectors and strain relief to 2x78 way D connector 
feedthroughs 

Attachment 2- pins of one of the four feedthroughs were damaged. Needs to be replaced.
Attachment 1: IMG_5056.JPG.jpg
IMG_5056.JPG.jpg
Attachment 2: IMG_5053.JPG
IMG_5053.JPG
  122   Wed Oct 13 15:28:22 2021 RSS TD + OGSplit funnels

Split funnels installed on 4 (of 8) 2x78 way D connector feed-throughs.

Attachment 1: IMG_5038.JPG
IMG_5038.JPG
Attachment 2: IMG_5039.JPG
IMG_5039.JPG
Attachment 3: IMG_5040.JPG
IMG_5040.JPG
Attachment 4: IMG_5041.JPG
IMG_5041.JPG
Attachment 5: IMG_5042.JPG
IMG_5042.JPG
Attachment 6: IMG_5043.JPG
IMG_5043.JPG
Attachment 7: IMG_5044.JPG
IMG_5044.JPG
  121   Wed Oct 13 15:16:12 2021 TDOrientation of 2x 78 way D connector feedthroughs
Looking downstream

Attachment 1 top right pair
           2 bottom right pair
           3 bottom left pair
           4 top left pair

PB "The long sides of the connectors on the 2 lowest flanges should be next to each other
and the short side of the connectors should be towards the motors."

The orientations of the other flanges do not matter.

'Long' cables to L-R connectors, 'short' cables to U-D connectors.
Attachment 1: 20211013_152518.jpg
20211013_152518.jpg
Attachment 2: 20211013_152529.jpg
20211013_152529.jpg
Attachment 3: 20211013_152549.jpg
20211013_152549.jpg
Attachment 4: 20211013_152606.jpg
20211013_152606.jpg
  120   Wed Oct 13 12:06:09 2021 RSS TDFlanges cleaned
RSS & TD had some success cleaning the COF600 flange surfaces of the staining and residues observed when the downstream COF600 section was opened yesterday  
https://elog.ph.ed.ac.uk/CARME/118

Isopropanol and laboratory tissues were used - most but not all of the staining and the residues were removed.
Attachment 1: IMG_5011.JPG
IMG_5011.JPG
Attachment 2: IMG_5012.JPG
IMG_5012.JPG
Attachment 3: IMG_5013.JPG
IMG_5013.JPG
Attachment 4: IMG_5014.JPG
IMG_5014.JPG
Attachment 5: IMG_5015.JPG
IMG_5015.JPG
Attachment 6: IMG_5016.JPG
IMG_5016.JPG
Attachment 7: IMG_5018.JPG
IMG_5018.JPG
Attachment 8: IMG_5019.JPG
IMG_5019.JPG
Attachment 9: IMG_5020.JPG
IMG_5020.JPG
Attachment 10: IMG_5021.JPG
IMG_5021.JPG
Attachment 11: IMG_5022.JPG
IMG_5022.JPG
Attachment 12: IMG_5023.JPG
IMG_5023.JPG
  119   Wed Oct 13 11:59:23 2021 TD[How to] Open COF600 copper wire seals
Use the M10 jacking points provided top/bottom and 
left/right on the upstream and downstream sides of the 
flanges - for example see attachments 1 & 2
Attachment 1: 20211013_103806.jpg
20211013_103806.jpg
Attachment 2: 20211013_103800.jpg
20211013_103800.jpg
  118   Tue Oct 12 13:54:21 2021 RSS TD + OD DRCARME opened
With the assistance of Oemer and Davide all of the M22 bolts removed from the downstream section of the CARME chamber. To separate the downstream section from the 
upstream sections it was necessary to use a lever between M10 bolts screwed into the lift points of adjacent sections of the CARME. The upstream sections were then 
lifted from the support frame and placed on the shipment crate base. The open ports of the CARME chamber sections were covered by Al foil.

Attachments 1-3 show downstream section following removal of upstream sections of CARME chamber. Note staining/residue top and bottom right - attachments 2 & 3.
Attachment 1: 20211012_143212.jpg
20211012_143212.jpg
Attachment 2: 20211012_143221.jpg
20211012_143221.jpg
Attachment 3: 20211012_143229.jpg
20211012_143229.jpg
Attachment 4: IMG_5002.JPG
IMG_5002.JPG
Attachment 5: IMG_4981.JPG
IMG_4981.JPG
Attachment 6: IMG_4982.JPG
IMG_4982.JPG
Attachment 7: IMG_4987.JPG
IMG_4987.JPG
Attachment 8: IMG_4989.JPG
IMG_4989.JPG
Attachment 9: IMG_4994.JPG
IMG_4994.JPG
Attachment 10: IMG_4999.JPG
IMG_4999.JPG
Attachment 11: IMG_4977.JPG
IMG_4977.JPG
Attachment 12: IMG_4996.JPG
IMG_4996.JPG
Attachment 13: IMG_5001.JPG
IMG_5001.JPG
Attachment 14: IMG_5002.JPG
IMG_5002.JPG
Attachment 15: IMG_5003.JPG
IMG_5003.JPG
Attachment 16: IMG_5004.JPG
IMG_5004.JPG
Attachment 17: IMG_5005.JPG
IMG_5005.JPG
Attachment 18: IMG_5006.JPG
IMG_5006.JPG
Attachment 19: IMG_5007.JPG
IMG_5007.JPG
Attachment 20: IMG_5008.JPG
IMG_5008.JPG
  117   Tue Oct 12 09:22:37 2021 RSS TD + OG DRMotors problem solved

Neg and ion cables were taken off and were put in the box.

Top support was taken off.

Motors are rotating again. Have to be careful with the position of the limit switches.

Attachment 1: IMG_4971.JPG
IMG_4971.JPG
Attachment 2: IMG_4970.JPG
IMG_4970.JPG
  116   Mon Oct 11 11:24:16 2021 RSS TD MLValve support and cable labeling

Split funnels were given to Oemer for cleaning. Have received them back after lunch.

Valve support is installed again (see picture 1).

Ion pump was connected but not activated. Michael will help in doing so. No vacuum support to help will RGA. Will proceed without it.

Neg and ion cables were labeled (see pictures 2 and 3).

Chamber was vented using nitrogen.

 

Attachment 1: IMG_4962.JPG
IMG_4962.JPG
Attachment 2: IMG_4969.JPG.svg
IMG_4969.JPG.svg
Attachment 3: IMG_4968.JPG.svg
IMG_4968.JPG.svg
ELOG V3.1.4-unknown